Enron Mail

From:chris.germany@enron.com
To:john.singer@enron.com, james.javins@enron.com, heidi.griffith@enron.com,dick.jenkins@enron.com, scott.hendrickson@enron.com
Subject:4 CNG Notices
Cc:mary.franklin@enron.com, angie.zeman@enron.com, victor.lamadrid@enron.com
Bcc:mary.franklin@enron.com, angie.zeman@enron.com, victor.lamadrid@enron.com
Date:Tue, 4 Apr 2000 03:56:00 -0700 (PDT)

OUTAGE REPORT FOR GATHERING Received 4/3/2000 2:35 p.m.
Posted 4/3/2000 2:35 p.m.


STATE: PA
FACILITY: Cherry Tree Station
PLANNED WORK: Overhaul Unit #2
OUTAGE DATE: April 10-20
FLOW REDUCTION: 2.4 MMCFD
CONTACT: Kevin Miknis
STATION PHONE: 724-468-3731

STATE: PA
FACILITY: Stoney Run Station
PLANNED WORK: Overhaul Unit #3
OUTAGE DATE: April 24 - May 5
FLOW REDUCTION: 2.0 MMCFD
CONTACT: Kevin Miknis
STATION PHONE: 724-468-3731

STATE: WV
FACILITY: Jones Station
PLANNED WORK: Overhaul Unit #1
OUTAGE DATE: April 17-20
FLOW REDUCTION: 1.0 MMCFD
CONTACT: Larry Wade
STATION PHONE: 304-477-3366

FACILITY: TL-263
PLANNED WORK: Replacement tie-ins
OUTAGE DATE: April 15
FLOW REDUCTION: 34.0 MMCFD
CONTACT: Steve Searls
STATION PHONE: 304-595-1270



Notice to all Appalachian Pool Operators: Received 3/29/00 2:00 pm
Reclassification Notice Posted 3/29/00 2:00 pm

On February 10, 1999, the FERC approved Docket No. CP97-549, granting CNG
Transmission's (CNGT's) request for reclassification of various transmission
lines to gathering lines. As part of that Docket, several transmission lines
were denied to gathering. On March 12, 1999, CNGT filed for rehearing to
further support the reclassification of the lines denied reclassification.
On March 21, 2000, the FERC approved Docket No. CP97-549-001, granting
reclassification of five lines from transmission lines to gathering lines.
The newly reclassified gathering lines include: D-2149, H-19921, LN-943,
H-124 and H-21777 south of Bradley Compressor Station. On March 22, 2000,
CNGT filed new tariff sheets to implement the reclassification effective
April 1, 2000. Although the FERC has not yet granted approval of the tariff
sheets, CNGT is notifying producers that upon approval of the new tariff
sheets, CNGT will begin charging a gathering rate of $0.198/Dt. and a fuel
retention of 2.28% for all gas moved on the lines listed above. If you have
questions regarding this notice, please contact Nancy Aucremanne at
(304) 623-8698 or Celesta Miracle at (304) 623-8262.

April 3, 2000 Received 4/3/00
11:10 am
Posted 4/3/00
11:10 am

Dear Pool Operator:

CNG Transmission Corporation (CNGT) plans to take its Hastings
Extraction Plant (H.E.P.) out of service to perform annual maintenance
starting at 12:01 a.m. on Tuesday, September 12, 2000. This requires
that the "wet gas" system behind the H.E.P. in West Virginia be shut in.
The plant shutdown will last approximately twenty-one (21) days if no
unexpected problems arise during the shutdown. Normal plant operations
are scheduled to resume on Tuesday, October 3, 2000. All questions
concerning the shut in and the subsequent turn in should be directed
to CNGT's local operations supervisor in the production area.

Unless other arrangements have been made to move gas to markets
other than on CNGT, all wet gas production must be shut in by 5:00 p.m.
on Monday, September 11, 2000. This will allow our compressor stations
to pull down the field pressure prior to going completely down at midnight
and will ensure that we maintain the time-lines on our schedule. As per
CNGT's tariff, failure to shut in by 5:00 p.m. will result in CNGT
considering
the gas to be unauthorized and it will not be credited as a delivery to your
pool.

As the exact time the plant will resume service is very difficult
to determine, and in an effort to minimize confusion, producers in your
pool will need to coordinate the turn in of their production with CNGT's
local operations supervisor. We are also asking that all pool operators
notify producers in their pool of this shut in. CNGT will not notify
producers individually.

We appreciate your cooperation and assistance on this. I also wanted
to you to know that we are attempting to complete all work necessary for us
to avoid shutting down the plant next year. The next regularly scheduled
shut down will not be until 2002.

If you have any questions about this letter, please feel free to
contact me at (304) 623-8698.

Sincerely,



Nancy M. Aucremanne
Manager, Producer Services
And Business Agreements


ANNUAL FACILITY OUTAGE SCHEDULE Received: 3/31/00 1:10 pm
April 1, 2000 through March 31, 2001 Posted: 3/31/2000 1:10 pm

Facility: Leesburg
Down Time: 3 Days
Out of Service Date: April ?
Back in Service Date: April ?
Reason for outage: Service Filter Seperator.
Remarks:
**************************************************************
Facility: Chambersburg Down Time: 1 Day
Out of Service Date: April ?
Back in Service Date: April ?
Reason for outage: Service Filter Seperator.
Remarks:
***********************************************************
Facility: Sweeney Station
Down Time: 2 months
Out of Service Date: June 1
Back in Service Date: August 1
Reason for outage: Automation of Engines (Will not effect customers)
Remarks:
**************************************************************
Facility: Cornwell - Unit #9
Down Time: Unknown
Out of Service Date: ?
Back in Service Date: ?
Reason for outage: Foundation Replacement, 8000 hr. inspection, general
maint.
Remarks:
**************************************************************
Facility: Cornwell (Entire Station)
Down Time: 1 Day
Out of Service Date: September ?
Back in Service Date: September ?
Reason for outage: Test Emergency Shutdown
Remarks:
**************************************************************
Facility: Cornwell #8 Unit
Down Time: 2 weeks
Out of Service Date: 9-11
Back in Service Date: 9-25
Reason for outage: 24000 hr inspection
Remarks:
**************************************************************





Facility: TL406
Down Time: 1 Month
Out of Service Date: 5-1
Back in Service Date: 5-31
Reason for outage: Installation launcher/receiver and new gate valves
Remarks:
**************************************************************
Facility: TL378
Down Time: 6 Days
Out of Service Date: June ?
Back in Service Date: June ?
Reason for outage: Replace road crossing.
Remarks:
**************************************************************
Facility: South Bend Station
Down Time: 6 Days
Out of Service Date: June ?
Back in Service Date: June ?
Reason for outage: Install new fuel filter
Remarks:
**************************************************************
Facility: Washington #2
Down Time: 5 Days
Out of Service Date: 4-10
Back in Service Date: 4-14
Reason for outage:
Remarks:
**************************************************************
Facility: Washington #1
Down Time: Currently
Out of Service Date: ?
Back in Service Date: ?
Reason for outage: Engine Inspection
Remarks:
**************************************************************
Facility: Groveport #1
Down Time: 12 Days
Out of Service Date: 4-17
Back in Service Date: 4-28
Reason for outage: General Maintenance (Main Unit)
Remarks:
**************************************************************
Facility: Groveport #3
Down Time: 5 Days
Out of Service Date: 5-1
Back in Service Date: 5-5
Reason for outage: Shutdown/Engine Inspection.
Remarks:
**************************************************************
Facility: Groveport #1
Down Time: 5 Days
Out of Service Date: 5-15
Back in Service Date: 5-19
Reason for outage: General Maintenance-Compressor
Remarks:
**************************************************************
Facility: Groveport #2
Down Time: 5 Days
Out of Service Date: 6-5
Back in Service Date: 6-9
Reason for outage: General Repairs..
Remarks:
**************************************************************
Facility: Groveport #3
Down Time: 12 Days
Out of Service Date: 8-7
Back in Service Date: 8-18
Reason for outage: General Maintenance (Turbo Charger)
Remarks:
**************************************************************
Facility: TL400
Down Time: 4 to 5 Days
Out of Service Date: June
Back in Service Date: October
Reason for outage: Road-crossing.
Remarks:
**************************************************************
Facility: Line 546
Down Time: ?
Out of Service Date: June
Back in Service Date: June
Reason for outage: Pigging preparations (Effect North Sheldon/Marilla)
Remarks:
**************************************************************
Facility: DeRuyter M&R
Down Time: 5 Days
Out of Service Date: 6-10
Back in Service Date: 6-14
Reason for outage: Replacement of measurement.
Remarks:
************************************************************** Facility:
LN-536
Down Time: 12 Days
Out of Service Date: 6-19
Back in Service Date: 6-30
Reason for outage:Replace 200 ft of pipe.
Remarks:
**************************************************************
Facility: LN-30
Down Time: 12 Days
Out of Service Date: 8-7
Back in Service Date: 8-18
Reason for outage: Installation launcher/receiver
Remarks:
**************************************************************
Facility: Newfield M&R
Down Time: 19 Days
Out of Service Date: 7-10
Back in Service Date: 7-28
Reason for outage: Rebuild entire station
Remarks:
**************************************************************
Facility: Freeville M&R
Down Time: 5 Days
Out of Service Date: 6-12
Back in Service Date: 6-16
Reason for outage: Replace Heater
Remarks:
**************************************************************
Facility: TL-342
Down Time: 1 Day
Out of Service Date: September ?
Back in Service Date: September ?
Reason for outage: Longwall Mining Repairs (Will not effect Customers).
Remarks:
**************************************************************
Facility: Hastings Extraction Plant
Down Time: 21 Days
Out of Service Date: 9-12
Back in Service Date: 10-3
Reason for outage: All Wet Production Shut-In
Remarks:
**************************************************************
Facility: LN-264
Down Time: 19 Days
Out of Service Date: 7-3
Back in Service Date: 7-21
Reason for outage: Pipe replacement. (All wet production south of Jones
Station)
Remarks:
**************************************************************
Facility: TL-422
Down Time: 19 Days
Out of Service Date: 7-3
Back in Service Date: 7-21
Reason for outage: Pipe replacement.
Remarks:.
***************************************************************

Note: Throughout the spring and fall, we will be conducting various shut-in
tests,
maintenance, and repairs on our storage pools. While we will make every
effort
to mitigate the effect of these tests, they could have some effect on our
overall operations.